NSEA-SR-146 (North Sea)

CHALLENGE

A major operator in the Danish North Sea required a plug to be set in the upper tubing of their well. The initial set of the plug did not pass the pressure test due to CaCO3 scale in the tubing. The customer considered using an i-broach & brushes on slickline and/or jet/bead blasting on coiled-tubing to remove the scale.

However, due to the successful use of BLUESPARK® to efficiently remove scale on 30 previous wells for the customer, the delays caused by mobilizing other equipment & the probable duration of the operation, they decided to immediately mobilize BLUESPARK® instead.

SOLUTION

Remove scale from the upper completion of the wellbore using electro-hydraulic pulsing technology.

  • BLUESPARK® equipment mobilized in 24 hours.

  • The BLUESPARK® 275 tool was transported by helicopter (including a complete backup set of tools) in a single flight to the rig (no special permitting required as there is no HAZMAT).

  • A 7.5 m (25 ft) interval was treated in an operating time of 6.25 hours.

Blue Spark Energy - case study BLUESPARK® Saves 4 Days Rig time North Sea

CONDITIONS

  • Depth: 115 m (375 ft)

  • Temperature: 20 °C (68 °F)

OUTCOME

  • Blue Spark Energy, the Wireline provider, and the client’s teams were able to load out the equipment and personnel in one day.

  • The modular, compact design of BLUESPARK® allowed the entire kit (with backups) to be flown in one helicopter trip.

  • BLUESPARK® cleaned the scale from the tubing section and tubing hanger, resulting is a successful plug set and test.

  • 4 days of rig time and considerable cost were saved.


Blue Spark Energy is paving the way towards a sustainable, dynamic oil & gas industry. As leaders in high-pulse powered wellbore remediations, we provide a revolutionary technology that is a safe, cost-effective, and efficient solution for forward-thinking energy providers.

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NSEA-SR-147 (North Sea)

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NSEA-SR-145 (North Sea)